Solutions to increase the C-2P well production performance at X oil field, Block 09-2

  • Affiliations:

    1 PetroVietnam Exploration Production Corporation, Hanoi, Vietnam
    2 Hanoi University of Mining and Geology, Hanoi, Vietnam

  • *Corresponding:
    This email address is being protected from spambots. You need JavaScript enabled to view it.
  • Received: 4th-May-2023
  • Revised: 6th-Sept-2023
  • Accepted: 30th-Sept-2023
  • Online: 31st-Oct-2023
Pages: 94 - 108
Views: 1151
Downloads: 16
Rating: , Total rating: 0
Yours rating

Abstract:

The well C-2P had its first oil production in July 2008, the initial production rate is 3,000 barrels/day. Due to the reservoir pressure depletion in 2017-2018, the well faced difficulties in kicking off to open the well for production. In November 2018, when the C-5PST2 well was put into production, the C-2P well was not produced by natural flowing. The kicking off has been attempted many times but the well still won't flow. The main reason the well couldn’t flow is due to low reservoir pressure which has not enough energy to push all the fluid in the well to the surface after each well shutdown. The flow assurance study shows, at the reservoir pressure of 3,000 Psi, and tubing head pressure of 950 Psi, the well can’t flow naturally. In addition, with the reservoir pressure of 3,000 psia and applying the gaslift injection rate of 1.0 MMscf/d, injection point at 3,030 mTVD, the well flowed. The continuous gaslift pump helps maintain the well's production in case the reservoir pressure drops even lower to 2,000 psi, and at the same time, optimizing the gaslift pump flow helps to increase the well production by 100-300 barrels of oil/day. When the reservoir pressure drops lower, it is necessary to lower the gaslift valve deeper to continue kicking off the well and maintain the well production performance. On the other hand, due to the lack of a gaslift valve for the original design of C-2P well so it's necessary to have gaslift tubing pack off in order to bring the well back to production, maintain stability and improve production. This paper, therefore, presents the results of the research on the solution to increase the production output of the C-2P well located in X oil field used gaslift valve combining with the tubing pack off. Results of the research on the application of solution show that the well's production output has increased significantly (0.354 million barrels) in the first year of applying the solution.

How to Cite
Do, K.Duy and Nguyen, T.Van 2023. Solutions to increase the C-2P well production performance at X oil field, Block 09-2 (in Vietnamese). Journal of Mining and Earth Sciences. 64, 5 (Oct, 2023), 94-108. DOI:https://doi.org/10.46326/JMES.2023.64(5).09.
References

Lê, P. H. (2006). Cơ sở khoan và khai thác dầu khí, NXB Đại học Quốc gia Thành phố Hồ Chí Minh.

Nguyễn, H. N. (2022). Khai thác dầu bằng phương pháp Gaslift.

Phùng, Đ. T., Dương, D. L., Nguyễn, V. C, Lê B. T. (1999). Công nghệ và kỹ thuật khai thác dầu khí, NXB Giáo dục.

Abdalsadig, M. A., Nourian, A., Nasr, G. G., and Babaie, M. (2016). Gas lift optimization to improve well performance. International journal of mechanical, aerospace, industrial, mechatronic and manufacturing engineering10(3).

Boyun, G., Xinghui, L., Xuehao, T. (2017). Petroleum Production Engineering. Second Edition. Gulf Professional Publishing. United States.

HVJOC, (2006). Báo cáo Tài nguyên dầu khí tại chỗ RAR mỏ X, Lô 09-2.

 HVJOC, (2007). Báo cáo Cập nhật kế hoạch phát triển mỏ PDP/EDP mỏ X, Lô 09-2.

HVJOC, (2008). Báo cáo hoàn thiện giếng khoan C-2P.

HVJOC, (2021). Báo cáo sửa chữa lắp đặt tubing pack off giếng C-2P.

HVJOC, (2022). Báo cáo Cập nhật kế hoạch phát triển mỏ FDP mỏ X, Lô 09-2.

Bugti, J. A. (2014). Optimization of gas lift system (Doctoral dissertation, Universiti Teknologi Petronas).

James, F. L, Henry, V. N and Mike, R. W. (2008). Gas Well Deliquification. Second Edition. Gulf Drilling Guides.

Other articles